NEW ORLEANS -- Oil giant BP PLC laid much of the blame for the rig explosion and the massive Gulf of Mexico spill on itself, other companies' workers and a complex series of failures in an internal report released Wednesday before a key piece of evidence has been analyzed.
The lead BP PLC investigator is saying that eight separate failures had to occur for the company's deepwater well to unleash the largest offshore oil spill in history.
At a briefing in Washington Wednesday on BP's internal investigation, Mark Bly, the chief investigator, told a room of reporters that all eight things needed to happen to cause the accident. The failures included cement that did not prevent oil and gas from entering the well and a blowout preventer that did not seal off the well.
The company's presentation at a downtown hotel was expected to last 90 minutes.
Bly also said that while the company's report was clinical and fact-based, the investigative team had 'a very strong emotional feeling about the accident.'
In its 193-page report posted on its website Wednesday, the British company describes the incident as an accident that arose from a complex and interlinked series of mechanical failures, human judgments, engineering design, operational implementation and team interfaces.
BP spread the blame around, and even was critical of its own workers' conduct, but it defended the design of its well and it was careful in its assessments. It already faces hundreds of lawsuits and billions of dollars of liabilities. In public hearings, it had already tried to shift some of the blame to rig owner Transocean Ltd. and cement contractor Halliburton. BP was leasing the rig from Transocean and owned the well that blew out.
The report was generated by a BP team led by Mark Bly, BP's head of safety and operations.
BP's report is far from the final word on possible causes of the explosion, as several divisions of the U.S. government, including the Justice Department, Coast Guard and Bureau of Ocean Energy Management, Regulation and Enforcement, are also investigating.
Also, a key piece of the puzzle -- the blowout preventer that failed to stop the oil from leaking from the well off the Louisiana coast -- was raised from the water Saturday. As of Tuesday afternoon, it had not reached a NASA facility in New Orleans where government investigators planned to analyze it, so those conclusions were not be part of BP's report.
The April 20 rig explosion killed 11 workers and led to 206 million gallons of oil spewing from BP's undersea well.
Investigators know the explosion was triggered by a bubble of methane gas that escaped from the well and shot up the drill column, expanding quickly as it burst through several seals and barriers before igniting.
But they don't know exactly how or why the gas escaped. And they don't know why the blowout preventer didn't seal the well pipe at the sea bottom after the eruption, as it was supposed to.
The details of BP's internal report were closely guarded -- and only a short list of people saw it ahead of its release.
There were signs of problems prior to the explosion, including an unexpected loss of fluid from a pipe known as a riser five hours before the explosion that could have indicated a leak in the blowout preventer.
Witness statements show that rig workers talked just minutes before the blowout about pressure problems in the well.
At first, nobody seemed too worried, workers have said. Then panic set in.
Workers called their bosses to report that the well was 'coming in' and that they were 'getting mud back.' The drilling supervisor, Jason Anderson, tried to shut down the well. It didn't work. At least two explosions turned the rig into an inferno.
Members of Congress, industry experts and workers who survived the rig explosion have accused BP's engineers of cutting corners to save time and money on a project that was 43 days and more than $20 million behind schedule at the time of the blast.
In its report, BP defended the well's design, which has been criticized by industry experts.
'The investigation team reviewed the decision to install a 9 7/8 in. x 7 in. long string production casing rather than a 7 in. production liner, which would have been tied back to the wellhead later, and concluded that both options provided a sound basis of design.'